Restoration Diary
Up to 10th October 2001 We're going to try and document as much of the rebuild of the M as possible. As we're actually seven weeks into the restoration at the time of writing much of the strip down has already taken place, but a lot of photographs have been taken, so we'll be able to show most of what has been done so far.
The initial aim was to separate the body from the chassis and treat them as two mini projects, as both need a lot of work. Preparation of the body for painting is going to take a lot of time and effort, so if we could get that right down down to the bare shell, we'd be better placed to work on it. This involved removing the interior and all fittings.
The
rear screen came out first, giving us easy access to the interior and fuel tank
area. The interior at the rear of the car isn't in bad shape, but we wanted to
get the carpets out to let us see what was what.
The
hardboard panels at the back came up easily, and the panel with speakers lifted
up to reveal the fuel tank All seemed in fairly good condition on first
inspection.
I
was surprised to see the two wooden struts going across the fuel tank, but
checking the parts list confirmed the M was actually built with these formed
into the GRP! The main problem with getting the carpets out was the mounting
bolts for the seatbelt reels. Bolts went through the bodywork and onto a strap
coming off the rear of the chassis. These were well rusted, and any amount of
effort would not shift them.
Still wanting to achieve something, we moved our attention to the front of
the car. The bonnet was very loose, so removing the hinge bolts was an easy job,
and gave us a lot more room in the single garage!
Work
on the bonnet itself is low priority at the moment, so this has been put into
storage under a tarpaulin in the back garden!
With a little more room to spare, we went back to work on the bolts at the back
of the car. We invested in a nut splitter in an attempt to get them off quickly,
but as the nuts were under the rear wheel arch, the angle we had to come in at
was very tight, and the splitter was not as effective as we would have hoped.
Victory was gained with the help of a set of bolt cutters and a cutting disc on
a Black and Decker multi tool. The two bolts on the other side followed soon
after, enabling the future removal of the carpets on the rear shelf and on the
rear arches.
We had the opportunity to borrow a
friends pressure washer, and although the weather was doubtful, we were able to
tow the M out onto my driveway and have a good go at cleaning up the wheel
arches and as much of the chassis as we could see.
There
was over an inch of mud in places, and a fair amount of oil in and around the
engine bay, so it was an ideal opportunity to get
a better view of the underside of the car. Some of the engine bay was also
cleaned out, particularly around the sump area, and the difference was amazing.
When
it comes to taking the engine out, a little gunk should clean things up nicely.
The chassis, at the front at least, doesn't seem to look too bad. There is of
course some surface rust, but as can be seen from the photo. the original paint
can be seen in some places. Suspension areas were all cleaned up and at the rear
of the car the diff was cleaned of as much as we could reach.
Next to come out was the fuel tank. We
had a suspicion that the interior was corroded, as when tapped, what sounded
like rust could be heard falling off the inside. The main pipe to the filler cap
area was very tight, but with copious amounts of Plusgas, the pipe eventually
slipped off. We never expected there to be any fuel in the tank, but on moving
it we realised that there was a small amount still in there. A bit worrying
considering we had been cutting metal very close to that area!
A
bit of a clue to the condition of the tank was the colour of the liquid inside -
a strange pale orange colour...! After
we fed the tank through the gap in the wooden struts, it became apparent that
there was some badly repaired crash damage on the o/s rear quarter. Although
very difficult to spot from the outside, the inside showed a very sticky area of
GRP, and a couple of self tapping screws holding the side light fitting on. The
bolt to hold the rubber bumper to that quarter looked relatively new too, and
was loose. We'll have to make a decision sometime about how stable this repair
is, and if we end up grinding it back and renewing it before respraying.
With
the weather slowly closing in, time to go back into the garage and look some
more at the interior. Wiring is a particular issue with these cars. The vast
majority of the wiring is black, and identification is by means of small rubber
bands slipped over the wires themselves. Over time of course, these bands come
off and identification is down to testing and wiring diagrams, so labeling of
any wires that were still connected was paramount. The dashboard was already
loose, so we started to disconnect it and label any wire we took off. Taking the
windscreen out made life a little easier, so we had access to the whole of the
back of the dash.
This
was in really good condition being fairly protected from the elements. The
center panel of the dash comes out, so moving forward it would be nice to
replace this with a decent wooden panel. All the instruments seem ok, but we'll
have to wait and see if they all work or not! This also seemed like a good point
to take the drivers door off, giving us a little more room to maneuver
around the car and work in the cockpit area. The fitted door is
damaged slightly at the front, but when we bought the car, Adrian gave us a
spare, which will be prepared for spraying with the rest of the car.
With
the dash disconnected, the only areas stopping us from removing the loom were
the steering column/ignition and the engine bay. The steering column would have
to be removed to take the body off anyway, so this seemed like a logical step to
take. with the steering wheel removed, the rest of the column was
straightforward to take apart, and this along with the column controls was
labeled and stored. The only remaining section is an 8" strut coming
through the bulkhead. Also in that area, the pedal box was removed, although
this needed a little persuasion.
A couple of swift hammer taps, and the entire
unit came away. This is in generally good condition, but the pedal rubber is
very well worn. This was certainly a well used car! The other main interior
fitting was the drivers seat itself. This looked to have been removed/replaced
fairly recently, as the bolts were quite new. I also found out why I had
problems getting myself into the car - under each of the seat mounting, there
were three wooden blocks, raising the height of the seat by about 2.5"!
Being 6' 8", suffice to say these won't be replaced!
Although
not connected to the chassis directly, to clear up the body for future work the
brake servo was removed. This was an easy removal after the fluid was drained
from the reservoir. The bleed nipple on the front
o/s wheel was loosened, and with some gentle pressure on the brake pedal, clean
fluid flowed freely. Although the brake piping will be replaced throughout, this
was a good sign.
After some deliberation, we have decided to leave the wiring loom in the car for the time being, as it goes through a hole and grommet in the bulkhead. We need to find out the best way of dealing with this before jumping in feet first.
As far as we can tell at the moment, this covers all the fittings that may connect body to chassis, apart from 15 or so rusted 25 year old bolts that is! Next job, body off!